Drivetrain Stock bypass valve/check engine light
Stock bypass valve/check engine light
I have a r56 MCS that has several modifications: Alta FMIC, Alta CAI, Greddy Type-rs blow off valve.
Ever since I installed them they have been running fine until..
Yesterday, I was driving around and pushed the MINI to about 6000 rpm, when I heard this loud pop. then the engine seemed to become sluggish and the stock bypass valve could no longer be heard. After parking and restarting the engine, the check engine light came on.
Im assuming the car's stock bypass valve blew or something.
Btw, the car runs normal (no stalling or awkward engine idling) after this event. Just the CEL is on. Also, no strange sounds or boost leaks seem to be heard.
Has this ever happened to anyone? anyone know of a solution or what the problem may be?
Ever since I installed them they have been running fine until..
Yesterday, I was driving around and pushed the MINI to about 6000 rpm, when I heard this loud pop. then the engine seemed to become sluggish and the stock bypass valve could no longer be heard. After parking and restarting the engine, the check engine light came on.
Im assuming the car's stock bypass valve blew or something.
Btw, the car runs normal (no stalling or awkward engine idling) after this event. Just the CEL is on. Also, no strange sounds or boost leaks seem to be heard.
Has this ever happened to anyone? anyone know of a solution or what the problem may be?
Last edited by Cawtou; Apr 6, 2009 at 11:34 AM.
I have a r56 MCS that has several modifications: Alta FMIC, Alta CAI, Greddy Type-rs blow off valve.
Ever since I installed them they have been running fine until..
Yesterday, I was driving around and pushed the MINI to about 6000 rpm, when I heard this loud pop. then the engine seemed to become sluggish and the stock bypass valve could no longer be heard. After parking and restarting the engine, the check engine light came on.
Im assuming the car's stock bypass valve blew or something.
Has this ever happened to anyone? anyone know of a solution or what the problem may be?
Ever since I installed them they have been running fine until..
Yesterday, I was driving around and pushed the MINI to about 6000 rpm, when I heard this loud pop. then the engine seemed to become sluggish and the stock bypass valve could no longer be heard. After parking and restarting the engine, the check engine light came on.
Im assuming the car's stock bypass valve blew or something.
Has this ever happened to anyone? anyone know of a solution or what the problem may be?
I see. I also for got to add that when I push it to around 3000 rpm, I can hear the installed greddy but still cant hear the stock dv
Greddy valves are notorious for leaking if they're not set quite right. Get the car scanned and look over all of your pipes, I really don't think you blew up your stock dv.
either way. something isnt right, since the stock dv is suppose to operate in normal boost conditions. I rechecked my pipes and seems like no leaks. idk. what do you think?
Last edited by Cawtou; Apr 6, 2009 at 12:00 PM.
just checked and seems like the tubes are fine. and sounds like there are no leaks when engine is running
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LOL. Yes. TUrbo to hotpipe, hotpipe to fmic, fmic to cold pipe, cold pipe to throttle body. Its one of those.
Check the hose coming off the turbo that goes to the intercooler. Chances are the clamp came loose from under it. It looks ok up top but under the silicon it comes off if you dont install it correctly.
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