Drivetrain The King is Dead, Long Live the Queen
The King is Dead, Long Live the Queen
My wife Kelli's MINI:


M45, RMW Tune, Head, CAM, Race Header and Exhaust, 17% Pulley, GP Intercooler, Brisk Silver Racing Plugs, Stock Coil, wires, and bottom end.
Worlds most powerful MINI on a stock blower and bottom end is now owned by a Girrrl


M45, RMW Tune, Head, CAM, Race Header and Exhaust, 17% Pulley, GP Intercooler, Brisk Silver Racing Plugs, Stock Coil, wires, and bottom end.
Worlds most powerful MINI on a stock blower and bottom end is now owned by a Girrrl
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The Jetta is pretty upgraded. I am going water/meth with it next, but I will spray it with a 100 octane program and it should put it right where she is with horsepower. I still have more torque than her, but I can't beat her handling
Then speak up Donkey
.
Correct me if I am wrong but Danny has the M45 record
.
Longboard
.Correct me if I am wrong but Danny has the M45 record
.Longboard
Last edited by batrugger; Sep 8, 2008 at 02:26 PM. Reason: Picture restored due to content.
IIRC, this car had parts from other vendors, right? And these parts have been replaced with OEM and RMW stuff.
I hope its a red wine tasting....
this car was extremely frustrating
this car had 175 across the board for compression and the leak down was good yet it was a poor performer
it had multiple problems that took quite some time to work through
the car had idling issues, throttle body codes, misfires you name it
we had this car on the dyno 4-5 times and the results were not as good as other cars with the same mods
No fear, Wes and Kellie were on board to make it right, the best part as they were open to doing what it takes to get it right. Kelli tracks her car and is looking to achieve her goals and I wanted to get this car right so she could set her goals even higher for next season.
Danny from MiniCorsa and I set out to change out the wiring /sensors until the electrical issues went away. It finally stopped throwing codes so we scheduled another tune day. You could tell the first time it ran up that things were different. It set a new personal best on the dyno. by the looks of the 245whp graph it had much more in it as I knew where the timing was before on the last tune. The car just wasn't happy and now with all of the electrical issues gone..... it wanted to run. So we added in some timing and fuel and there goes 255whp........ hmmmm.... a few more tweaks later and 263whp and then we ran it even hotter and it laid down 267whp.... It was a great experience getting this car to heights once thought unattainable. Thanks again to Kelli, Wes and Danny for hanging in there when things weren't going the right way. It just shows what perserverance can do
congrats and see you at the track!!!
this car had 175 across the board for compression and the leak down was good yet it was a poor performer
it had multiple problems that took quite some time to work through
the car had idling issues, throttle body codes, misfires you name it
we had this car on the dyno 4-5 times and the results were not as good as other cars with the same mods
No fear, Wes and Kellie were on board to make it right, the best part as they were open to doing what it takes to get it right. Kelli tracks her car and is looking to achieve her goals and I wanted to get this car right so she could set her goals even higher for next season.
Danny from MiniCorsa and I set out to change out the wiring /sensors until the electrical issues went away. It finally stopped throwing codes so we scheduled another tune day. You could tell the first time it ran up that things were different. It set a new personal best on the dyno. by the looks of the 245whp graph it had much more in it as I knew where the timing was before on the last tune. The car just wasn't happy and now with all of the electrical issues gone..... it wanted to run. So we added in some timing and fuel and there goes 255whp........ hmmmm.... a few more tweaks later and 263whp and then we ran it even hotter and it laid down 267whp.... It was a great experience getting this car to heights once thought unattainable. Thanks again to Kelli, Wes and Danny for hanging in there when things weren't going the right way. It just shows what perserverance can do
congrats and see you at the track!!!
Congrats on the impressive numbers! How easy are the burnouts now? LOL
I'm jealous of the GP intercooler, MINIUSA won't let any more of those out in the wild anymore
What ended up being the corrective action to get the engine happy? Was is one of the sensors that was being flakey?
I'm jealous of the GP intercooler, MINIUSA won't let any more of those out in the wild anymore

What ended up being the corrective action to get the engine happy? Was is one of the sensors that was being flakey?
Congrats on the impressive numbers! How easy are the burnouts now? LOL
I'm jealous of the GP intercooler, MINIUSA won't let any more of those out in the wild anymore
What ended up being the corrective action to get the engine happy? Was is one of the sensors that was being flakey?
I'm jealous of the GP intercooler, MINIUSA won't let any more of those out in the wild anymore

What ended up being the corrective action to get the engine happy? Was is one of the sensors that was being flakey?
wiring harness and map sensors for sure
Congrats on the impressive numbers! How easy are the burnouts now? LOL
I'm jealous of the GP intercooler, MINIUSA won't let any more of those out in the wild anymore
What ended up being the corrective action to get the engine happy? Was is one of the sensors that was being flakey?
I'm jealous of the GP intercooler, MINIUSA won't let any more of those out in the wild anymore

What ended up being the corrective action to get the engine happy? Was is one of the sensors that was being flakey?
Last edited by batrugger; Sep 6, 2008 at 02:12 PM.




