Drivetrain AWE MINI F5X S-FLO Carbon Intake. Available now!
I have this intake and have to say it was well worth the wait .
I tried to order it direct and was told I had to use awe europe as I live in the UK but that one did not work out after a two month wait as my intake did not go in there container so I imported one my self from out motoring and had it in a week happy days.
I tried to order it direct and was told I had to use awe europe as I live in the UK but that one did not work out after a two month wait as my intake did not go in there container so I imported one my self from out motoring and had it in a week happy days.
We have confirmed the AWE S-FLO Carbon Intake to fit the 2019 MSC (2-door and convertible models) as well as JCW models!
Josh - I picked up the intake used from a friend and am experiencing a P00BD code for "Mass Air Flow (MAF) A Circuit Range/Perf Flow Too High." Friend did not have any codes in the approx 8000 miles he used it. Everything looks to be in perfect shape and installed easily following AWE's instructions. Any idea what the issue could be?
Josh - I picked up the intake used from a friend and am experiencing a P00BD code for "Mass Air Flow (MAF) A Circuit Range/Perf Flow Too High." Friend did not have any codes in the approx 8000 miles he used it. Everything looks to be in perfect shape and installed easily following AWE's instructions. Any idea what the issue could be?
Josh - I picked up the intake used from a friend and am experiencing a P00BD code for "Mass Air Flow (MAF) A Circuit Range/Perf Flow Too High." Friend did not have any codes in the approx 8000 miles he used it. Everything looks to be in perfect shape and installed easily following AWE's instructions. Any idea what the issue could be?
Although the last thing I want is more airflow at this point - CEL says I already have too much
Just an update on the CEL issue I was having... I brought the car into the dealer and had it smoke tested. Turns out the charge pipe was faulty and causing a vacuum leak. It was replaced under warranty and after about 300+ miles of driving I can report the CEL has not come back. Normally it would come on within 10 miles of clearing it. Kind of strange that the CEL was only triggered with the aftermarket intake installed and ran totally fine on the stock airbox. I guess the leak coupled with the increased airflow was enough to trigger it while the leak with the stock box must have still been within spec for some reason.
Just an update on the CEL issue I was having... I brought the car into the dealer and had it smoke tested. Turns out the charge pipe was faulty and causing a vacuum leak. It was replaced under warranty and after about 300+ miles of driving I can report the CEL has not come back. Normally it would come on within 10 miles of clearing it. Kind of strange that the CEL was only triggered with the aftermarket intake installed and ran totally fine on the stock airbox. I guess the leak coupled with the increased airflow was enough to trigger it while the leak with the stock box must have still been within spec for some reason.
Hi josh
if I was to change one thing on your design of this CAI it would be to add a rubber grommit to the retaining arm were the bolt goes through just like the stock air box as what I find is that the retaining bolt works loose because the CAI cannot move with the engine.
if I was to change one thing on your design of this CAI it would be to add a rubber grommit to the retaining arm were the bolt goes through just like the stock air box as what I find is that the retaining bolt works loose because the CAI cannot move with the engine.
Hi josh
if I was to change one thing on your design of this CAI it would be to add a rubber grommit to the retaining arm were the bolt goes through just like the stock air box as what I find is that the retaining bolt works loose because the CAI cannot move with the engine.
if I was to change one thing on your design of this CAI it would be to add a rubber grommit to the retaining arm were the bolt goes through just like the stock air box as what I find is that the retaining bolt works loose because the CAI cannot move with the engine.






